Hello,
I hope you're doing well.
I recently watched the Drone Tracking Radar: Part 7 – Longer Range and MTI Processing video and get the same radar used in the demonstration. I attempted to replicate the experiment using the Range_Doppler_Plot.py script from GitHub, but the output appears much noisier compared to the results shown in the video. The difference is significant.
We have tested the setup in multiple environments with minimal interference, yet the noise persists. We suspect the issue might be related to calibration files, but we are unsure. Have others encountered similar issues? Could the problem be linked to calibration?
We would greatly appreciate any guidance, as we are currently stuck at this stage.
